Ok... long story but after replacing the head stock belt on a Delta 46-465, which as per the directions involved me whacking the spindle in a vain attempt to get it moved out of one side of the head stock to replace the belt, I put the chuck on the lathe last night and there was a noticeable wobble. Tonight I put a dial indicator on the headstock spindle and measured ~ 12 1/1000ths out of true. I can't swear it was always like this since I've mostly used the chuck at turning class. Turning between centers seems to be ok - a trued cylinder tonight didn't seem to have much runout. but I am certainly willing to concede I screwed it up. Is there a way to fix this? My Google-Fu is not strong tonight on finding suggestions for fixing it. Am I strong enough to have bent the spindle while it is still inside the stepped pulley? I used both a rubber mallet and a framing hammer with a wood block.
Learned today that the chuck could be installed on the outboard side of the lathe also, so put it there and no wobble. Next I put a 1" 8 tpi nut on the inboard side spaced off the spindle nut then jammed the chuck against that, no wobble. Next I took off the spindle nut and noticed a bit of munging around where a wrench slipped at one of the points. Turned it around, put the chuck against the wrong side, no wobble. filed down the munge, put the spindle nut back on and no wobble. :gar-Bi
Learned today that the chuck could be installed on the outboard side of the lathe also, so put it there and no wobble. Next I put a 1" 8 tpi nut on the inboard side spaced off the spindle nut then jammed the chuck against that, no wobble. Next I took off the spindle nut and noticed a bit of munging around where a wrench slipped at one of the points. Turned it around, put the chuck against the wrong side, no wobble. filed down the munge, put the spindle nut back on and no wobble. :gar-Bi